START HERE |
|
Register | FAQ | PM | Events | Groups | Blogs | Calendar | Mark Forums Read |
Unregistered
|
4G6 / V120 Series Walkera 4G6 / V120 Series Helicopter Support |
|
LinkBack | Thread Tools | Display Modes |
03-06-2014, 11:44 PM | #1 (permalink) |
Registered Users
Join Date: Dec 2013
|
V120D02S V2 weakish tail holding...
Hello
I've noticed lately that my tail isn't holding as well as it used to. If I quicklyish move the rudder stick left right left right, the tail will blow out. This has caused 1 crash. Also when I'm flying backwards or sideways, the tail isn't locked in and the heli turns in whatever direction it feels like. It's ok with flips and all that though... Just not feeling very locked in. All gears are good. I have good tail pitch. My main blade pitch isn't too high/low (around +/-11) and I run a flat 100 in idle up (which is what I fly in). Also I'm pretty sure my gains are good... It's at 70 in my TX and the rudder dial on the gyro is at about 4 o'clock. Is this normal? Am I just over exagarating? I'm going to upgrade my V120 to 2 cell and get a GY280RX, but I want the tail to hold well before I do anything to it. Oh also, why can't I change rudder travel in my DEVO 7? I can change the numbers but it doesn't do anything to my servo travel...? Thanks, Hamish
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
Sponsored Links | |||
Advertisement |
|
03-07-2014, 12:13 AM | #2 (permalink) |
Registered Users
|
Turn the rudder EXT all the way up it will increase servo range. You will also then be able to further increase/decreae the range via TX. Change the tail boom also you'll be amazed at what a difference that makes. It's probly cracked under tail box or servo mount.
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 12:21 AM | #3 (permalink) |
Registered Users
Thread Starter
Join Date: Dec 2013
|
Oh it's a brand new boom, the old one lost is strength and it was twisting.
And by 4oclock I mean the EXT is around as far as it can go. Can't go any futher ;-) Thanks, Hamish :-)
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
03-07-2014, 12:32 AM | #4 (permalink) |
Registered Users
|
I raised travel ADJ RUDD to 125 in my Tx (7e) and the piro rate was too fast so I lowered it back to 112. Anything over 125 and the servo would kick back the wrong way at the end of travel. My gain (TX) is at 76.5% I think you could bump yours up a bit.
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 12:35 AM | #5 (permalink) |
Registered Users
Thread Starter
Join Date: Dec 2013
|
Ok well I'll try raising the gain, but won't be able to test for awhile (after the weekend) as it's raining now and in going away in the weekend.
I'll get back to you ASAP! Thanks, Hamish :-)
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
03-07-2014, 12:48 AM | #6 (permalink) |
Registered Users
|
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 03:59 AM | #7 (permalink) |
Registered Users
Thread Starter
Join Date: Dec 2013
|
I managed to squeeze a small flight in before I left, the rain managed to hold off. Raising the gain has make things a lot better, still not the best in backwards flight but good enough.
Thanks for your help heli yea! Hamish
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
03-07-2014, 12:58 PM | #8 (permalink) |
Registered Users
|
The last trick in the book move the servo up/down the boom to correct rotation. Tini tiny movements like half mm test then adjust push rod if needed. repeat steps as needed to get it perfect. Its alot of toying around but worth it. mine is rock soild on hard pitch pumps fast forward/backward.
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 01:50 PM | #9 (permalink) |
Registered Users
Thread Starter
Join Date: Dec 2013
|
I've also done that, but I can't seem to move it a small mm each time, it's to tight on the boom and I have to push hard so it "jumps" around the boom, no small movements.
Did you test yours in adjustment mode? How do you know when it's spot on? Thanks, Hamish :-)
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
03-07-2014, 02:55 PM | #10 (permalink) |
Registered Users
|
NEVER TEST FLY IN ADJ MODE. You dont need to be in ADJ MODE for this. First set the TX gyro gain to 50% the RX light will go out. Adjust the push rod till blades have 0 pitch. Raise the TX gain to back to your setting test fly by punching the throttle if the nose turns left, lengthen 1 full turn/test turns right shorten the rod. Moving the servo gives you a half turn when needed. The magic spot is found by luck and lots of tinkering/testing. Oncw it holds fly it backwards and fine tune the TX gain till it is perfect.
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 03:20 PM | #11 (permalink) |
Registered Users
|
part 2 perfect gain
Raise the TX gain till the tail "wags" in hover flight then lower TX gain .5 to 1 point at a time till the "wagging" stops. Now fly backwards and fine tune .5 at a time so you have a good hold and no wag. If you're not getting a good hold, go back to adjusting servo position and rod length.
BTW you only use ADJ MODE when turning the pots on the RX w/power, of course.
__________________
-Heli Yea! Master of: the living room, mechanical setup and, the obvious! Belt'ish CP FBL, HDX 500 DFC, New V120D02S FBL, Mini CP FBL, Hirobo Shuttle ZX, 450L w/VX1e, QR-X350PRO FPV, 450L w/APM FPV(in progress) DEVO 10 white w/2km range! |
03-07-2014, 10:58 PM | #12 (permalink) |
Registered Users
Thread Starter
Join Date: Dec 2013
|
Awesome, I'll have a good tinker when I get home.
Thanks for the detailed instructions Hamish :-)
__________________
Goblin 700 Black Thunder-Xnova XTS 4525 560kv- BK7001HV/BK7006HV- Hobbywing 130a V4- Spirit Pro Citizen 828 |
Thread Tools | |
Display Modes | |
|
|